This motor has always started quickly with no problems until the last 2 seasons. Last year, I replace the key switch when the motor would not start. I determined with conductivity tests that the switch was bad. Also replaced waterpump and prop shaft seals. I replaced a bowl on one of the carburetors that was leaking at the BB on the bottom of the bowl. I ran a can of OMC engine tuner through the motor and let it soak overnight. I do this annually. The motor would not start the next day until I installed new plugs. It started and ran normally after the plugs were installed. Subsequent starts were difficult, sometimes not starting until the plugs were cleaned. I ultimately changed the plugs and it ran fine for the rest of the season.
This year I did not run engine cleaner through the motor as I probably did not put 10 hours on the motor since the last cleaning. I did have a bad kill switch and replaced this. I also replaced another carb bowl for a leaking gasket surface. I am running QL77JC4 plugs.
I have been premixing oil since the motor was about 2 years old. I drained the gas about a week ago and put new gas in the motor and changed the plugs. Still having cold start issues. The motor acts like it is flooding. When I pull the plugs they are coated with oil. I can clean them and reinstall and the motor starts and runs well with no restart issues. This motor has alway started well with no issues. The only difference is that it is on a lift in a boat slip for the last 2 years. Prior to that it was kept under a carport. I would appreciate any help you can give me on this problem.