04 225 HO DI motor, rebuilt 30 hrs ago, has been running great until past week. Has what appears to be a slight base gasket leak (oil on midesction after storing) which I was getting ready to fix - then it developed a miss last weekend, worse today. Happens only after motor has run perfectly normal at speed for 5-10 mins then gets progressively worse, to where it misses/bogs even at 1000 rpm, but generally idles fine. Hooked up software and 12/40V outputs are fine, CPS checks out, exhaust pressure varies with throttle as problem occurs. Circ pump (priming) and lift pump pressures (at idle) check out fine, as does lift pump vacuum, no water in filter. The apparent temp dependence has me thinking coil or coils - what do y'all think? Need to check coil and circuit resistance and primary voltage but couldn't these be normal unless measured when the problem is happening? Hard to do. Appreciate expert insight into this problem.
Just to make things even more "interesting" I found the head of an upper crankhead bolt in the belly pan - definitely not overtorqued during rebuild, what in the world could cause this? There is zero wobble at the flywheel.
Computer was repaired 5 hrs after rebuild by DFI - oil injector circuit short.
Looking forward to getting these issues behind me!![]()