Decent bag of fish, making the 60 mile run back from the mouth of the Suwannee River up to the Santa Fe River for weigh-in and to try to cull a couple of the smaller ones before weigh-in time. Strolling along at 5600 RPM when suddenly a loud BOOM and rattling. Look back, cowling is shaking and smoking. At first I thought I spun the prop out and limiter shut the motor down, but trimmed up and prop was good to go.
Used trolling motor to get to the side of the river to a sandbar and took the cowling off, just to see if anything was unusual. Now, I am not a marine mechanic or motor expert, but something told me that 4-inch gash in the engine block with smoke coming out of it wasn't supposed to be there!
Mercury has been awesome, sending a new powerhead from Wisconsin and will arrive today, dealer will have it installed this weekend and have me back on the water early next week to break it in. Just wanted to share. No idea what caused it, Mercury is planning to do a full breakdown to determine the cause.
And the obligatory beer-for-scale picture...
Everyone is safe, wasn't scary, nothing in the logs to indicate any errors. She just went Tango Uniform! Fortunately, another boat in the tournament picked up my partner to go weigh-in our fish, and he got the truck to come pick me up. Motor blew about 100 yards upriver from a public boat ramp, so I got to troll down to it, tied off, sat on the boat in the warm Florida sun, and turned some Bob Marley on, smoked a Cohiba, and drank beer for an hour until my partner got there. I should break down more often!
Moral of the story: Always, even if you don't plan on using them all, HAVE AN 18-PACK OF BEER IN THE COOLER!
Will update when Mercury determines the cause, if they let me know.
UPDATE: Mercury has not told me what happened on original motor. I don't expect they will.
New powerhead arrived 2 days after I dropped it off at shop. Tech put it on and called me Friday to come get it for break-in. I carried to the river that weekend, and boat would not crank. Turned over, no catch. Back to shop Monday morning, had zero compression on #4. BRAND NEW POWERHEAD.
So, motor #2 goes back to Mercury and motor #3 is shipped out. Motor 2 arrives Thursday this past week, tech puts it on. This time he puts one hour on the motor at a lake to verify. After lots of mistakes and miscommunication, I have her back and going to break in more today.
Third powerhead in 2 weeks...