Thread: Low rpm

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  1. #1
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    Low rpm

    2011 merc proxs with 2014 power head model#1B974945 wot 5200 rpm 25 fury not a prop problem. Had sleeves checked, they are ok. runs good but cant get over 5200 any expert advice would be appreciated

  2. Member
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    Huntingtown, MD
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    #2
    Was the 14 tuner used with the powerhead?
    04 521VX 250 Pro XS
    14 521C 250 Pro XS

  3. Member
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    #3
    Not sure. Why?

  4. Member
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    #4
    Anybody check to see if you're, in fact, achieving Wide Open Throttle?

  5. Mercury 3L/4 Stroke/Verado Moderator EuropeanAM's Avatar
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    Greenville, SC (US)
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    #5
    That was simply a rotating assembly (powerhead)- so there would not have been any need or reason to change the exhaust tuner.

    Start with the BASICS:

    -Compression Test
    -Spark Test
    -Fuel Quality, Delivery, and Air/Fuel Pressure Tests
    -Record fuel and air pressures at idle, under acceleration, and 5/10/15 seconds after shutdown
    -Verify engine reaching WOT at linkage
    -Test tensioner spring with INCH lbs torque wrench. Set at 70 lbs/in, it should click before reaching end of travel (if not, REPLACE SPRING AND BELT)
    -Inspect Reeds
    -Inspect exhaust tuner and powerhead gaskets (rough view with bore scope with gearcase removed)


    Dual Mercury Master Technician- for Mercury Outboards, Mercruiser and Mercury Racing at European Marine in Greenville, SC.
    Still consider myself a "Marine Apprentice" after 47 years (learn something new every day).
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  6. Member
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    #6
    ill have him check all of that and get back. Thanks

  7. Member
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    #7
    checked tuner and gaskets, all ok tech found 1 bad fuel injector and compressor had over 1000 hrs on it so im changing that out. crossing my fingers