https://streamable.com/stwxps
Serial 1B5xxxxx. So I had another thread a short time ago when I had my motor cutting off (when cold, first cranked, and put into gear). Anyway, I ended up pulling my plugs (2-3months old) and gapping them to .032-.033 - they had indeed been too closely gapped. The idle was better and I only had 1-2 stalls when switching into gear - still not normal I guess but better idling and less cutting off. Yesterday started acting up again - wouldn't stay running at idle coming back to dock. All coils were showing spark through spark tester but pulling the direct injector harness on #3 showed no effect whatsoever. Today, same thing when cranked so I put in an old original plug I had in #3 and it idles fine now. Is the mist coming from the video above normal? Why did the plug go bad? Here's a pic of the plug I just removed from #3: https://ibb.co/FWmgtfx